Analysis of information sources in references of the Wikipedia article "British Airways Flight 38" in English language version.
The CVR and FDR have been successfully downloaded at the AAIB laboratories at Farnborough and both records cover the critical final stages of the flight. The QAR was downloaded with the assistance of British Airways and the equipment manufacturer.
Initial indications from the interviews and Flight Recorder analyses show the flight and approach to have progressed normally until the aircraft was established on late finals for Runway 27L. At approximately 600 ft and 2 miles from touch down, the Autothrottle demanded an increase in thrust from the two engines but the engines did not respond. Following further demands for increased thrust from the Autothrottle, and subsequently, the flight crew moving the throttle levers, the engines similarly failed to respond. The aircraft speed reduced and the aircraft descended onto the grass short of the paved runway surface.
As previously reported, whilst the aircraft was stabilised on an ILS approach with the autopilot engaged, the autothrust system commanded an increase in thrust from both engines. The engines both initially responded, but after about 3 seconds, the thrust of the right engine reduced. Some eight seconds later the thrust reduced on the left engine to a similar level. The engines did not shut down and both engines continued to produce thrust at an engine speed above flight idle, but less than the commanded thrust.
Recorded data indicate that an adequate fuel quantity was on board the aircraft and that the autothrottle and engine control commands were performing as expected prior to, and after, the reduction in thrust.
All possible scenarios that could explain the thrust reduction and continued lack of response of the engines to throttle lever inputs are being examined, in close co-operation with Boeing, Rolls-Royce, and British Airways. This work includes a detailed analysis and examination of the complete fuel flow path from the aircraft tanks to the engine fuel nozzles.
Safety Recommendation 2008-047: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency, in conjunction with Boeing and Rolls-Royce, introduce interim measures for the Boeing 777, powered by Trent 800 engines, to reduce the risk of ice formed from water in aviation turbine fuel causing a restriction in the fuel feed system.
Safety Recommendation 2008-048: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency should take immediate action to consider the implications of the findings of this investigation on other certificated airframe/engine combinations.
Safety Recommendation 2008-049: It is recommended that the Federal Aviation Administration and the European Aviation Agency review the current certification requirements to ensure that aircraft and engine fuel systems are tolerant to the potential build-up and sudden release of ice in the fuel feed system.
The CVR and FDR have been successfully downloaded at the AAIB laboratories at Farnborough and both records cover the critical final stages of the flight. The QAR was downloaded with the assistance of British Airways and the equipment manufacturer.
Initial indications from the interviews and Flight Recorder analyses show the flight and approach to have progressed normally until the aircraft was established on late finals for Runway 27L. At approximately 600 ft and 2 miles from touch down, the Autothrottle demanded an increase in thrust from the two engines but the engines did not respond. Following further demands for increased thrust from the Autothrottle, and subsequently, the flight crew moving the throttle levers, the engines similarly failed to respond. The aircraft speed reduced and the aircraft descended onto the grass short of the paved runway surface.
Safety Recommendation 2008-047: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency, in conjunction with Boeing and Rolls-Royce, introduce interim measures for the Boeing 777, powered by Trent 800 engines, to reduce the risk of ice formed from water in aviation turbine fuel causing a restriction in the fuel feed system.
Safety Recommendation 2008-048: It is recommended that the Federal Aviation Administration and the European Aviation Safety Agency should take immediate action to consider the implications of the findings of this investigation on other certificated airframe/engine combinations.
Safety Recommendation 2008-049: It is recommended that the Federal Aviation Administration and the European Aviation Agency review the current certification requirements to ensure that aircraft and engine fuel systems are tolerant to the potential build-up and sudden release of ice in the fuel feed system.